Ok guys.....did the leak down and the boss intake was a bubble factory. Ether or carb cleaner would NOT find the leak. It was leaking everywhere. I sealed it with black rtv neatly no gobs and let it sit all day and tightened it down. It ran like a screaming banshee!!!! Ended up with 56 pilots and 167 mains and 2 turns out on airscrews with the CE L int the 4th notch. Idles perfect and is crisp all the way through with topend out of this world. Thanks for all the help.