ok swapped everything back and forth one at a time(besides carbs, stock) double checked boots, put my buddies set of working stock reeds in. it runs the same. took it all apart did a leak down lost 2psi in 10min. so whats left? stator side crank seal sucking the air in but not blowing out? maybe the choke plunger letting air in? i sprayed all the possible areas with carb cleaner besides the crank seal, didnt bog. am i on the right track? any other ideas? might just take it all apart split the cases and reseal everything, its an 03 never been split
stock stroke, flotek dune port, put the timing at stock for now, stock carbs 340, 4th richest clip, 30 pilots, stock reeds, (chariot reeds and billet intake on the way) still off on the jetting but not to worried about that right now