06BCBANSHEE Posted February 16, 2013 Report Posted February 16, 2013 banshee was running like shit , took the carbs apart and cleaned them. they were filthy btw. dirtiest carbs I have ever seen. it seemed to bog at 0-1/4 throttle. It had 280 mains 30 pilot, needle 3rd clip i believe. sea level; right now its about 50 degrees ; summer about 68-86 FMF fatty gold series, chopped silencers, +4 timing, K&N air filter with power lid. Vforce 4 reeds. from what I have read 280 seems a little lean? I dropped the pilot to 27.5 and it elliminated the bog. Seems to rev and run great. planned on going riding tommror and doing a plug chop. Think its to lean on the main? input appreciated Quote
250rbanshee Posted February 16, 2013 Report Posted February 16, 2013 Plug chop is the best way to tell if its lean or not. I run 280 mains, stock pilots, and needle on the 4th clip year round. I don't ride in the cold weather much. My elevation is around 650. Throw in a set of 300 mains and see how it feels. Quote
apeik Posted February 16, 2013 Report Posted February 16, 2013 chances are...that dirt/sand whatever got into your motor if the slides got that dirty inside Quote
sheerider11 Posted February 16, 2013 Report Posted February 16, 2013 My girlfriend runs 27.5 290 with pods sea level. Quote
06BCBANSHEE Posted February 16, 2013 Author Report Posted February 16, 2013 chances are...that dirt/sand whatever got into your motor if the slides got that dirty inside Ya I was worried about that. I got my TORS kit installed by a motorcycle mechanic last summer. I was stupid and at the time was very uncomftorable with working on carbs. Which I know is very stupid, they are so easy. I inspected what I could, doesnt look like any sand got in the cylinders, there was no trace of anything where the reed valves go in. Comprerssion is at 124& 122. If sand and shit was gonna cause a problem it should have happened by now right? have only been able to ride for about 20 mins or so. Ill be doing a plug chop tommoro hopefully, It had these jets in it since I bought it, about 4 yrs ago, and just today I dropped the pilot to a 27.5 I also removed the overflow bottle, its now leaking a bit, will this stop once it drains a bit? I got a ASI rad ready to install, just aiting for my new steering stem so I can do both at once. thanks guys. It seems to run great now, ill post pics of my plug chop. Quote
Larry's Shee Posted February 16, 2013 Report Posted February 16, 2013 Make sure you have the rubber gaskets under the carb caps Quote
06BCBANSHEE Posted February 16, 2013 Author Report Posted February 16, 2013 Ya i checked for the gaskets, pretty sure the idiot that installed the TORS didn't completely tighten down the caps properly. the lock nuts on the caps was loose as well. which i could see it allowing dirt in. I should have just done everything myself. had no faith in myself at the time tho. It honestly runs great now, and my compression is good so I dont think I damaged anything. Time will tell I suppose. Quote
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