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Posted
So why did you stop running these? They were low on compression?
Did you check ring end gap
Long story short= I was inpatients dump cunt lol.
Fucked the crank which fucked the cylinder. On flywheel side cylinder there is a crack on the intake side of it, lucky it lost compression before it broke off completely. When I pulled it apart I could not believe how lucky I was.

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Posted
Seems kinda like a pretty light trail/mx type port. Not much real internal transfer work. 
Thanks, it was pulling nice when it was running,but nothing to crazy. For rebuild I went with stock jugs, added 21cc cool head and +4 timing plate and it feels actually faster with this set up than with that port work.

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