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bansheebrian06

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  1. Im lookin for clear clutch covers, could anybody tell me where you got you'rs from and how much? Thanks
  2. all banshee kicker's vibrate like that. I personally love that sound.
  3. Well i screwed with it today, and it just runs the same. Im just goin to take it to the local shop and let them do it. Looks like no riding for me this weekend!!
  4. Thanks alot guy's!! Im gonna play with it tomorrow and let you's know how it goes. Im probably gonna run 270 main jets with the air screw 1.5 turns out and the needle on the 4th clip and see how it goes from there.
  5. Thanks guys, im goin to switch the jetting tomorrow to 270 and see how that is, any suggestions on what size pilot i would need? Oh and i pulled the plugs and they are like a dark brown color and the quads smokin really bad.
  6. Thanks for all the help guys!! I hope i can help you's out one day. It idle's fine. Just as soon as i get on the gas it either stalls or runs ok if i keep the rev's up. But it still doesnt move too good, its like ridin a lawn mower, lol. Im still thinkin i need to move the clip up some and see how it runs. I just wanna make sure its not nothing stuppid before i go and do it and its not it.
  7. I have the snorkel off already, i really dont want to take the airbox lid off (due to problems with the kfx because of that) The choke tube is on, and i think the air screws are at 2.5 turns out. It starts bogging right from take off, it has no power at all, it barley moves.
  8. I jetted it to 240, its not running rite at all. It seems like its getting way too much gas. It has no powerband and it just bogs down and stalls. I moved the needle clip up one on the one side (didnt have enought time to do the other yet) and that side seems to run alot better. Any advice on how many i should go up with the needle? Or anything else i can do?
  9. Any time man, Did you try it and see if it worked at all?
  10. Thanks alot, im going to try the 240 that came with the quad. Anything else im gonna have to play with to get it right?
  11. I am putting my fmf fatty's and powercore 2 silencers on along with a twin air air filter with the snorkel removed. What should i run as fas as jetting? The local dealer told me to run it 20 more than it is which would make it 240. Is this right?
  12. It's ok, you need to pop out the black connector the cable is connected to with a flat screwdriver, once you get it off you will see a needle looking thing, it is spring loaded, so you can push it in, hold the needle in and see how it runs, if that is the problem you can either splice the wires and connect them, or just shove cardboard or something into the place where the black connector goes into the clutch perch so it will push in more and stay in better. If you need any more help with it let me know, im glad to help a fellow rider out in any way.
  13. I would give it gas and it would either bog or rev out really quickly without alot of throttle. Its right on the clutch perch, you will see the wire. You will need a screw driver to push the tab so it comes out. Even if this is not the problem its good to fix it before t causes you problems. Im goin to take mine off and cut the wires and put them together. The same thing went on my kfx. Look at this picture, it is the only cable comming out of the perch. http://i16.ebayimg.com/05/i/06/e9/ac/08_1.JPG Good luck with everything. Let me know if that works or not.
  14. Almost the same thing happend to mine today, it turned out to be the clutch sensor on the handlebars. If it does it again take it off and push the spring thing down and see if it runs then. Make sure the spring is totally in.
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