Jump to content

Eric_C1

Members
  • Posts

    21
  • Joined

  • Last visited

Posts posted by Eric_C1

  1. If I push and pull on my shift shaft there is a little play there which I believe is normal, could be wrong. But if its skipping teeth I would say something is wrong. I would take it apart and refer to these videos to make sure you have everything in there correctly.

     

     

  2. I had nearly the same jetting on my stock cylinders so you shouldn't be that far off. are the carbs synced? choke tube in? do you still have the tors on it? I know tors can cause issues like that. If it idles good and starts easy I wouldn't change the pilots.

    How do your plugs look? check floats and clean the carbs out to make sure nothing is clogging the jets. I'd also do a leakdown to rule out air leaks. 

  3. Did you put the choke tube between the carbs back in after rebuilding the carbs? how did it run before the carb rebuild? 

    Do you have a carb sync tool? I would make sure they are properly synced after rebuilding. 

    If they are synced and it ran good before the rebuild I would do a leakdown test to make sure you're not sucking in a bunch of air through the intake gaskets that were just put on. I've found that you need to use sealant on the intake gaskets or else you'll be sucking excess air in. 

  4. Thanks for the info, is it because of the bowl size of the carbs? just can't keep up with how much more gas it goes through? would a dual pingle solve this issue? 

    I have FMF fattys on it now which i'm guessing are not the best pipe for the motor but i'm trying to keep the build under 3k so maybe i'll just upgrade those later. 

    How do you like yours in the woods? would you go with a different set up? 

  5. I'm looking to build a 421 serval cub setup and was just wondering if anyone had experience with this motor in the woods, how does it do in the tight stuff? the place I ride is mainly pretty fast open trails but there are some hill climbs with not much of a run up and some sorta technical areas.

    I was also wondering how this motor does with stock carbs, will they be enough for now? 

    and lastly what size domes will be safe with +4 timing and pump gas? The places I ride are between 450' and 750' of elevation. 

     

    If anyone rides this motor in the woods I'd appreciate your opinions, thanks 

     

  6. Took the shee on her maiden voyage this season and and it didn't last very long, after warming her up I started doing some pulls and noticed that she was cheechin real good out the right side pipe, shut it down and let it cool off, started it back up and was smoking normal again so I did a another pull on it and after getting warmed up she started smoking pretty bad again. Checked the head gasket and I don't see any leaks on it, it didn't seem to lose any fluids but I wasn't riding that long. Plugs looked very black and wet so shes definitely rich but I always run it rich and never seen it smoke like this so i'm thinking the crank seal is blown, also noticed there's a nice little pool of oil behind my front sprocket so guess that seal took a shit too. If it was my crank seal would it effect how the engine runs? cause it runs completely normal besides the extra smoke. Had a head gasket blow before and you can instantly notice a drop in performance but I didn't notice anything this time. Is there anything else I should check before before splitting the cases? really hoping I don't have to but all the signs point to the crank seal so it might just have to be done. If anyone has any ideas before I break her open that'd be great. 

     

    My mods are 

    FMF pipes, pod filters, +4 timing. This was the first ride after adding the +4 timing plate so i'm thinking this had something to do with it.

    290 mains, 3rd clip, 27.5 pilot 

×
×
  • Create New...