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TroyBrock

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Posts posted by TroyBrock

  1. Not sure where I should post these but this seems like a good spot. Recently bought a bunch of parts, which included lt250r and honda atc 350x parts. Among the parts were a pair of Works dual rate shocks with no ressy. I'm not sure what they go to because they are roughly 12.5" which is much too short for ltr shocks and obviously aren't atc shocks. I've looked all over and couldn't find anything. If any one has any ideas what they go to I'd appreciate it.

  2. It's running great, only thing I've found wrong with it so far is a crack in the nerf bar, gonna pull it off and weld it this winter. I've put a good 20 hours on it so far so if anything engine or suspension wise was messed up I think I would have noticed it by now.

  3. I had a trail tech vapor on my machine and for the most part it worked. The Tach was accurate, it went up and down about 200 rpm but it says right in the manual that it is only so accurate. The water temp worked great, the temp light was especially useful. You can even program a shift light for new riders, or for yourself. I never set up the speed sensor because it was on an 87 and the kit was made for 90 to new. The ambient temperature read out is nice and it even has a digital clock. 

  4. At the time the Banshee was running great, started right up first kick every time, only thing that it needed at that point was a new swing arm, which I had but didn't put on yet and a carb rejet because of the changing weather. I was just sick of things breaking every time I fixed something else, that particular banshee liked to be in pieces.

     

    the 4 poke has a shit ton of power compared to a stock banshee motor, obviously.

  5. Hey guys, quick background before I get to the problem. I recently fixed the idle gear and put in a new clutch, did everything to specs, used 3 HD and 3 regular springs and it was adjusted right. First few days it was great, then I noticed it was starting to be alittle jerky when I shifted from neutral to first, then it got real bad so I decided to take off the clutch over.

    Now here's the problem, 2 broken inner hub bolt holes and 2 other spring screws had started to back out. And the idle gear once again lost it's clip. I have a new inner basket and idle gear ready to go. I know the springs are suppose to be tighten to 7 lb/ft but I'm wondering what I can do to make sure this doesn't happen again. And if anyone might have and insight into what happened the first time.

     

    Thanks

    Troy

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