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jpaegel

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Everything posted by jpaegel

  1. not sure i will have to pull it out. and check. this was sent to be jetted already for the 2 into 1 set up is what they told me. moving the clip down should help out, i will try that and check to see what the pilot is
  2. ZillaFreak what set up are you running? it ran fine with the stock carbs before i tore it down. think the stock mikuni's i had 280/290 mains in them, and it ran like a raped ape. got the 2 into 1 for a heck of a deal and really want to use it. any trouble shooting pointers would be great
  3. yes 35mm pwk. it is running lean, plugs are white. checked for a intake leak already. it is really bugging me on what is wrong. i had a 38mm pwk but trinity said it was too large for a stock motor it had a 178 main and it was still lean. im ready to pull my hair out. stock motor boysen pro stock reeds pro circuit exhaust
  4. what jets are you using with your 2 into 1 intake. im having problems jetting mine and need a little help. i have a 35mm also and the 190 main is not enough, just dont want to buy a ton of jets to find what i need. thanks
  5. they say the 38mm is too much for my set up, is there truth to this or are they just trying to get me to buy a carb? just trying to get it back running without going back to stock carbs.
  6. i called trinitry and they said i should use a 35mm carb with my stock setup. needle clip is on #2 and just put new gaskets on, but i will check for leaks
  7. plugs are white
  8. think its a 55 pilot and 146 needle
  9. i have a 1991 banshee stock motor with pro circuit exhaust, trinity 2 into 1 intake with a keihin 38mm carb, boisin pro stock reeds. the main was a 165 that someone drilled out to .078. the problem i am having is the plugs are running hot and it is falling on its face. where should i start at and does anyone have a same set up
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