ok, i was railing it first to second and left off and pulled the clutch and there was little to nothing there, so i took it to a shop by haspen acres in indiana( cause thats where i was) and he said i burnt the clutch up and it was out of adjustment. so i put a new clutch in it and adjusted it and it worked, but then it started to get to about 130 and it did the same thing on me. it did have water in the oil when i took off the cover cause of that o ring leaking. whats the deal? it is built the guilt, it has a lockup clutch in it but its still the stock clutch, its bored 100 over full race jugs tripple ported, cool head etc.