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nicebanshee

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Everything posted by nicebanshee

  1. i have a 01 shee .080 over ported,cool head 21cc domes,billet impeller,boost bottle,no tors, stock carbs 27.5 330, uni pods, dinatek cdi i was running the trails this weekend here in fl bike was running great then i noticed i was getting a lil hot i let it cool down started riding again had no problems i was idling and the bike shut off i went to start it and the kick was completly stuck so i figured i was in for a rebuild took it all apart pistons and jugs are good took them out but crank is still stuck i can not move it at all the bike is in neutral i also noticed the domes turned black on the inside of the water passages found that a lil weird ive only had the cool head for about a week i was wondering if ne 1 had an idea of what could be going on
  2. i went and rode with the 330 it ran great top end a lil boogish bottom i did a couple runs then a plug chop came up nice light chocolate i am at 1.5 turns 3rd clip what is a good range on the airscrew.
  3. out riding!!!!!!!!!

  4. i got some 330s im gna go throw them on and go do a chop and go from there hopefully im somwhere close
  5. 01 shee with coolhead 21cc domes, t5s, dinatek ign, uni pods, trail port, .080 over, alum impeller, aftermarket crank bearings, durablue axle, itp rims, +2 swingarm, dg bolt ons etc............

  6. cool im gna pick up the 320s today and do a plug chop ill let yall know what happens thanx.
  7. i have a o1 banshee with coolhead 21cc domes, uni pods, dynatek ignition, toomey t5s, tors removal, it is bored .080 and trail ported i run klotz 40:1 93 oct. I am in florida my mains are 280 and i am 1.5 turns out i was told to run 300 or 320 does that soud about right i have stock carbs please let me know what sounds best
  8. so i w my local riding spot my bike was running fine then all of the sudden i realised i was overheating so i starded to head back tomy truck my bike started smoking really bad out of my left pipe i ran it untill it shut off (i only rode for about 20 min) i added water then when i tried restarting it i noticed coolant leaking out of the head bolts i took it home took the head out and noticed the gasket is bad but my cylinders look fine the only thing is that with the head off if i kick it water is coming out from the bottom of both pistons is this normal with the head off or am i in for a rebuild? also how do i know what piston i need i noticed some pistons are for long rod and is wiseco the best way to go?
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