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Posted

just got her back together...new everything on top

I was running a 180 main with the stock porting, and I can't seem to get enough gas to this thing. I keep going up on the main jet and it signs off too early. I have a 205 in it and it pulls strong up to around 6500 rpm then the power falls off in a hurry.....plug looks good, but there has to more pull left in it. Any of you guys running a 2-1 with porting have any ideas? I'm going to pick up some bigger jets tonight.

 

trinity intake---38 PWK

trail port

dek needle..3rd clip

52 pilot

4500' elevation

205 main ....pulls strong but does not rev out far at all

Posted

When I ported my motor, the std. DEK needle didn't have enough taper to let the main really give it the fuel. I had to go to an EEK needle. Same exact needle except the taper is steeper so it comes on to the main a tad sooner and lets it give it more fuel at 3/4 to WOT. My machine ran much better that way. I was up to a 230 main with the DEK and backed off to 205 with the EEK.

 

Give CarbParts.com a call and tell you need that needle. They'll get it to you quick.

Posted

sounds like the same thing to me, I got it running good and reving out nice after I put a 225 in it. I will get a EEK needle and keep tuning. Thanks for the help!

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